Case Studies
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Documents
Presentations
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Anode
Rodding Case Studies
Rod Shop Spent Anode (Butt) Stripping
Press/Crusher
Problem
The butt stripping press could not strip and break-up a butt over a
certain thickness. Up to 10% of the butts had to be routed to a manual
crusher to strip a large spent anode.
The manual crusher was very labor intensive and consumed man-hours that
were not available. The alternatives were to increase manning to
increase the through put of the manual crusher or to replace the
stripping press via a capital project of over $1 MM.
Action Taken
EFI worked with a team of production
and maintenance employees and identified the root cause of the problem
as the guillotine crusher blades stalling on thick anode butts.
EFI designed blades using surface
hardened steel with serrations to increase the crushing pressure. The
first iteration tested solved the stalling problem and reduced hydraulic
pressure but produced large pieces that the downstream crushers could
not process.
The team designed and tested a second iteration that produced more
fracture lines & smaller pieces.
Benefit
The solution provided reduced the hydraulic pressure of the crusher
which reduced the amount of breakdowns of the crusher. Also, larger
butts were able to be processed which relieved the need for increased
manning on the manual crusher.
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Dust Containment at Chain
Flail Butt Cleaner
Problem
The seal between an oscillating conveyor and the discharge hopper from a
chain flail butt cleaning machine failed excessively.
A failed seal caused an unacceptable dusty atmosphere in the Rod Shop
and an unacceptable buildup of material in the conveyor pits which
clogged the conveyor and resulted in conveyor and butt cleaning machine
outages.
Action Taken
The seal materials that were used were fabric and/or elastomer. Working
with the Carbon Area Maintenance team, EFI
prototyped a labyrinth metal seal that successfully survived a 6 month
trial. EFI also performed air flow
measurements on the Butt Crushing Material Handling Dust collector.
Benefit
EFI completed a design drawing
package for a complete retrofit of the seal. The airflow measurement
work did result in increasing the fan speed and resultant air flow by
15% at no capital cost. The atmosphere in the rod shop became
significantly better.
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Green Mill
Case Studies
Green Mill Dry Scrubber
Problem
Industrial Hygiene standards required that the scrubber be certified as
satisfying the design guidelines in the Industrial Ventilation Handbook.
Action Taken
EFI performed measurements, sketched
changes for numerous pick-up locations, and identified fouled ducts.
After cleaning and duct modifications were completed,
EFI certified compliance with the
Industrial Ventilation Handbook.
Benefit
Implementation of all changes recommended by
EFI resulting in significantly improved fume collection and a
certifiable system.
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Material Handling Case Studies
Improve Reliability of Ore Delivery to Pots
Problem
Anode effect rates were high due to upsets in the alumina delivery to
the pot. Alumina is delivered to the pot through a series of level air
slides directly to the pot feeder.
Actions Taken
EFI worked with process engineers,
operators, and maintenance personnel in the potline and fume control
departments and determined that there were multiple issues that kept
alumina from getting to the pot feeder.
- EFI
determined that many of the air slides at the pots are fouled on the
clean air side.
- Established that the pot air slide
blowers have been “slowed down” starving the air slides for volume
and pressure.
- EFI
established that the venting and lack of air space for the main
supply air slides caused the slide to be operated at high pressures
which causes cracking of the welds in the slides.
- EFI
worked with process engineers and pot operators, established that
the ore delivery valve behaves differently for “excessively fine
ore”, i.e. less ore is delivered per “shot”.
EFI performed a study and proved
that the pot feeders were sensitive to angle of repose of the
alumina which made the feeder shot weight less and variable when an
excessive amount of fines are in the alumina.
- Working with potline mechanics and
electricians, EFI prototyped
level control for the large main supply air slides.
- EFI
demonstrated the effect of “grit” on the pot air slide by setting up
an offline air slide with Plexiglas cutouts.
Benefits
- As a result of the work from
EFI, a routine daily sampling and
testing system for alumina in various locations in the alumina
transport was established. The alumina was tested with a flow
funnel. The data was used as additional information to adjust base
feed rates to the pots to reduce the number of anode effects and not
over feed the pots.
- Air pressure to the main supply air
slides was reduced which reduced the amount of leaks in the slides
from crack welds.
- A means to control compressed air
purge of the clean air side of the air slide was prototyped.
- The dust collector at the rail car
unload station was being investigated to the capture the superfines
and remove them from the good alumina stream.
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Anode Cover Material Delivery
Problem
Anode crust was delivered from the crushing system to potlines through a
dense phase system. The dense phase system had a very poor history of
reliability with excessive down time. This resulted in a very poor plant
bath balance.
The pots had a deficit of bath which required a lot of manual labor to
crust. The % alumina in the anode cover material was roughly 80 – 90%.
At times the crust silos became too full due to the lack of crust
transport, so that material had to be taken out of the silos.
Actions Taken:
- EFI
with process engineers performed a mass balance of anode cover and
crushed bath to establish what alumina percentage is possible in the
anode cover material with the current dense phase system at various
operational availability levels.
- Performed empirical measurements on
cover establishing actual practice.
- Established the existing transport
rate for the crust dense phase conveying system.
- EFI
applied the Failure Mode and Effects Analysis to the dense phase
conveying system for crust and established a future transport rate.
- EFI
performed a reliability analysis with operators and maintenance
personnel and established a direction to solve the various problems
in order of priority of impact on uptime.
Benefits
- As a result of the work from
EFI, a much better understanding of
the crust delivery problem developed. The studies showed that the
dense phase, even at 100% uptime was not capable of delivering the
amount of material required to attain a 50%/50% crust to alumina
composition for anode material needed to improve the plant bath
balance.
- EFI
established that a supplemental means for crust transport was
required.
- EFI
developed concept sketches and budget costs for the supplemental
crust transport. The solution was less than $70K.
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Potline Case
Studies
Prototype Improved Butt Reference
Anode Setting Method
Problem
Anode setting to an even horizontal plane was done by referencing the
butt removed from the pot. This was done by an operator transferring a
chalk mark from the rod of the butt to the rod of the new anode. This
method can not be audited for correct position in the pot. Also the
variation of the amperage traveling through all of the anodes was great.
This variation is expressed by the coefficient of variation of the anode
loads.
Actions Taken
- Established inaccuracy of current
method using a manual chalk mark transfer.
- Developed the concept of using the
anode setting mast on the PTM as the reference to set anodes .
- Developed concept of using an
encoder mounted on the anode mast that measures the travel of the
mast. 1 PTM was modified for test. A computer stored all of the
various positions of the mast during anode setting.
- Performed testing over 9 pots for 2
anode cycles.
Benefits
The concept was successfully tested by the prototype. Measurements of
anode current loading for the 9 test pots were compared to 9 control
pots show a 10 point reduction in the coefficient of variation. The
measurements stored in the computer enabled an audit of each anode
setting. Also, the measurements enabled a butt thickness of every anode
set.
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Improve Metal Tapping
Problem
An excessive amount of bath is drawn into the hot metal tapping ladle
which causes the ladle to be cleaned more often and also clogs various
equipment in the casting facility.
Action taken
EFI identified that
vortexing of the liquids were the critical issue.
EFI developed concepts and procedures
to reduce that vortexing during metal tapping including:
- Control the tapping rate by
controlling rate of compressed air to the venturi.
- Redesign the tapping tube to
increase open area of the tube intake thereby reducing velocity.
- Accurately control the height of the
tapping tube below the metal/bath interface.
- Working with the pot operators,
EFI performed baseline testing that
established a lower limit to the amount of bath tapped per pound of
metal tapped.
Benefit
Successfully proved concept for further plant trials and implementation.
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Improve Pot Scoop
Problem
The Scoop didn’t “reach” far enough into the pot and wasn’t able to
thoroughly clean the anode hole and retrieve all the dropped carbon
pieces. Also, the pneumatic cylinder rod routinely fails.
Action taken
EFI redesigned the Scoop utilizing
many of the existing components.
Benefit
One scoop was modified and put into service and performing as expected
and improved the anode hole cleaning process. All scoops were modified
with EFI’s recommended changes.
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Improve Pot Scoop Stand
Problem
When stored in its stand, the Scoop has twice fallen “back into the PTM
cab” resulting in one serious injury.
Action taken
EFI redesigned the Stand so that the
scoop will always fall away from the PTM
Benefit
One redesigned Scoop Stand was put into service and performing as
expected. All scoop stands were modified with
EFI’s recommended changes.
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Anode Hauler
Problem
Rear brakes failed to release quickly resulting in damaging tires. Also
the bed showed fatigue failure.
Actions taken
- EFI
troubleshot the brake circuit and tested design change using an
adjustable sequence valve.
- EFI
also examined the fatigue failures and altered design drawings.
Benefit
- One anode hauler brake circuit was
modified and placed into service and performed as expected. Orders
were placed for materials to modify the other anode haulers.
- EFI
completed detailed fabrication drawings for the anode hauler bed.
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Miscellaneous PTM Cab Improvements 1
Problem
Existing windows foul/scratch easily and caused poor visibility for the
crane operators.
Actions Taken
EFI located a hard coated
polycarbonate material. With a team of production and maintenance
personnel, EFI tested the material.
The team feels the improvement is significant.
Benefit
All PTM front windows were replaced with the new material.
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Miscellaneous PTM Cab Improvements 2
Problem
The fixed steps/ladder damage the removable pot hoods during anode
changing.
Actions Taken
Working with the Pot Operators, EFI
designed a folding ladder.
Benefit
Design was accepted by plant for implementation.
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Miscellaneous PTM Cab Improvements 3
Problem
The PTM cab ventilation system ingests excessive pot fumes due to the
location of the fresh air inlet.
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Actions Taken
EFI worked with the Pot Operators
and the Maintenance HVAC crews. EFI
prototyped a concept to alter the location of the ventilation pick-up to
a point closer to the louvers on building sidewall.
Benefit
Concept and prototype was successful and ready for plant implementation.
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Transport Ladle Handling
Problem
New hot metal transport ladles could not be turned with the existing
turning device so that the ladle can be cleaned.
Action Taken
EFI worked with the Potline Services
Crew and determined what modifications were required.
Benefits
EFI modified the fixture design &
certified the structural design drawings.
The solution was implemented quickly and minimized the disruption of the
process of cleaning transport ladles.
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Cast House
Case Studies
Continuous Homogenizing Oven Cooling Rate
Problem
The time required to cool down the homogenizing oven was a Cast House
production constraint.
Action taken
EFI engaged the OEM (Hertwich) and
established that it is possible to “force feed ambient air” into the
oven significantly reducing cool down time.
Benefits
Supplemental fans on order. When implemented the Cast House homogenized
billet cooling time can be reduced from more than 24 hours to12 hours.
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Casting Pits Fall Protection
Problem
Several previous fall protection design concepts at casting pits were
not successful.
Action taken
With a team of Casting Operators, EFI
sorted out the issues.
Benefits
The team accepted the Concept sketches for implementation in the plant. |